[QUOTE="Eric"] The pulley holding tool at the etoolcart site looks very much like the one that's illustrated in the manual. However, the honda manual also specifies that there's a special socket that's to be used with this tool, http://tinyurl.com/3bbuk. I didn't see this socket available at the etoolcart site. It might be worth your while to call them and inquire about the socket. It could be that they intend for you to use your own socket. For that to work, you'll need to know the inside diameter of their tool and find a socket that will work.[/QUOTE] I looked at the drawing at the UK site more closely and see what you mean. I also read George's and your subsequent posts. If I still needed the retail tool, I'd likely inquire about the diameter of the socket hole's dimensions. Onto the better news. :-) Yesterday I had an idea for modifying Eric's version of the tool so that the tool's steel bar does not touch the power steering pulley lip. It consists of Eric's design plus four lock rings and some rubber hose on each bolt. The lock rings and hose act as spacers and a protector so the bolts don't impose a force on the power steering pulley's lip. From right to left as one is standing at the front of the car, looking down, it's: 7/16" (pulley holding tool) bolt head, 4 lock rings, rubber hose over 7/16" bolt, crankshaft pulley, 7/16" nut. I didn't let the 2 foot steel bar push against the suspension or car's frame. Instead, I let the non-pulley end push against a pile of four 1/2" plywood boards on the ground. With a 5 foot extension pipe over the 1.5 foot long breaker bar, I proceeded slowly, intermittently checking to see that the bolts weren't pressing against the lip of the power steering pulley. They did not. After applying I estimate about half my weight, the pulley bolt broke free easily. I heard that huge, loud metallic crack that everyone describes. Some dust rose. I checked for damage; none was evident. I pushed with the 18" breaker bar alone, and sure enough the bolt was free. I estimate it took around 300 ft-lbs. of torque to break the bolt free. I did apply a little PB Blaster penetrating oil to the pulley bolt two days ago. The last time the bolt was removed was three years ago. It looks in good shape. JB Weld seems to be holding the chunk that chipped off the other day together fine. I did find a salvage yard that is pretty sure they have a 91 Civic crankshaft pulley for . I am still thinking of replacing the pulley and still have some concerns about the harmonic balancer. Had an amusing word from a dealer yesterday morning. I called Dealer Parts to see if by chance they had the retail pulley holding tool. They said no and then added that my troubles might be that the bolt is a left-hand thread. Ha. I said nothing, in the name of good relations, or because dealers are what they are. For the archives again: Early 1990s Honda Civic (or all Honda?) crankshaft pulley bolts are right-hand threaded = right tight and left loose). Total cost of my 1991 Civic LX 1.5 liter crankshaft pulley holding tool was under as follows: One 3/8" thick, 2' flat steel bar (a surveying stake, technically), Lowe's = .27 Two 7/16" diameter, 3" long, Gr. 8 fine thread bolts, True Value Hardware = .50 (or thereabouts) Two 7/16" diameter, Gr. 8 fine thread nuts, True Value Hardware = </body>.50 (or thereabouts) Eight 7/16" diameter Gr. 8 lock washers, True Value Hardware = </body>.04 Three inches of 1/2 " ID, 3/4" OD 200 PSI Goodyear hose, Lowe's = </body>.50 (or thereabouts) As Eric has described, drill the 7/16" diameter holes in the steel bar at one end, 3 inches apart. Snug up the nuts on the bolts as much as possible. There was still a little play when I started torquing but to no adverse effect, and the play will help assemble everything. I strongly recommend using two high quality 1/2 inch diameter, 10-inch long extension drives and a breaker bar at least 1.5 foot long, supported by a jack, as shown in part in the 4th photo from the top at site http://www.cadvision.com/blanchas/54pontiac/honda.html . Have strong, long pipe you can put over the breaker bar to give yourself a longer torque arm without risking life and limb. Of course I had to buy various new tools for this project, like a 7/16" titanium-coated drill bit ( at Autozone) and a 17 mm 1/2 inch drive deep socket (.50 at Pep Boys) and the usual minor wastage purchases of bolts, nuts, tools that don't work (few bucks) while I figured out how to make this all work. (BTW, I ran some numbers for the stress on a 3/8" drive setup. Don't do it. Breaking something is highly likely.) I am delighted with this success. Thanks especially to Eric, George, Curly, E. Meyer, Lex, Tom, Tegger and others who offered their experience on this matter over the last few months. Also, thanks to Gene Blanchard for his web site (link above). Onto the seals and various and sundry maintenance around the cam and crankshafts.